I am refurbishing a swing arm and couldn't find a "show and tell" for the swing arm bearing removal and replacement so am taking the opportunity to do it now.
It is usual fairly obvious when the bearings need replacement either through sideways movement of the swing arm when its in the TTR or when the bearing shaft and bearings look like this!
Because I dislike this job, and don't like to struggle unnecessarily, I had a stainless steel bar made up specifically to drive out the swing arm bearings. However, old screwdrivers, punches and steel tube/bar can be improvised as drifts to do the job!
It was cold in the garage this morning so I had a small propane heater running. I had a minor brainwave and used this to get the swing arm hot before tackling the bearing removal. In the past I have used a blowtorch to heat the bearing housing up.
Apparently aluminium expands three times that of steel as you warm it up although that doesn't always seem to be the case for me
The procedure is to put your drift into the swing arm from the opposite side to the bearing to be removed, locate the drift on the inner bearing race edge and drive out the bearing keeping a lot of sideways force on the drift to make sure it doesn't slip off the bearing edge.
It wasn't to be my lucky day as the first bearing drifted out easily but the second wouldn't budge. I have now managed to break off all of the inner bearing edge so the drift has nothing to purchase on or drive against.
I always find it best at this stage to go indoors for a cuppa and think about what to do next
Can you use a breaker bar (to save damaging the extension bar) long extension bar and socket (that just fits inside the swingarm) and hammer to drift it out from the outer race of the bearing?
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2000 TT-R250M-
Spoiler
Ported & polished, 73mm bore, Wizeco piston, US header pipe, FMF Q4, #150 main jet, #52.5 pilot jet, throttle stop screw adjusted, larger snorkel, GYT-R air filter, NGK Iridium spark plug, 14/51 gearing, NOS +
That might work Jarrah - I will give it a go another time.
I have managed to get the bearing out using a combination of strategies.
First off I used a worn (therefore small diameter) cutting disc in the Dremel to put a cut in the bearing shell to weaken it.
I then had a go at it with a small sharp cold chisel and hammer. The bearing casing is very hard and I managed to shatter a few pieces off and weaken the bearings grip on the swing arm just a tad. I then got the blow lamp on the swing arm housing and got it as hot as I could. I then sprayed WD40 onto the bearing shell to shock it and further help "crack" its adhesion to the swing arm.
There was just enough of a lip left on the inner edge of the bearing for the drift to catch on and this time it was possible to drift it out quite easily.
This is the outside edge of the bearing:
This is the inside edge showing the lip that I had left to get the drift on.
The swing arm is now fully stripped and power washed (not a nice job as it's very cold here today) ready for rubbing down and spraying.
Hopefully fitting the new bearing and seal kit will be the easier part of the job
Ok - so I tidied up and sprayed the swing arm and today set about fitting the new bearings. Took a bit longer than expected as I also rebuilt the linkage arm at the same time.
I use All Balls kits and the pic below shows what's in it. Shame they don't include the end caps as the RH one on this swing arm had started to get chewed up by the chain as the chain slider had worn through However, knowing this, I keep a small supply of new ones in stock
The pic below shows the worn out chain slider and you can just see on the swing arm end cap wear the chain had started to chew into it.
First off is to fit the bearings in the swing arm and I do this by squeezing the bearings in as far as I can using the vice. You will see that the bearings have different shaped "ends" and I assume that you are meant to push the bearings in using the wider "flat" ends.
I have an aluminium driver that does the job perfectly but used to improvise with sockets.
The bearings are recessed by about 3mm - not sure why but I press them in as Mr Yamaha intended!
It makes life easier to refit the linkage arm before the swing arm.
There will now be a slight delay whilst I clean up and re-attach the swing arm fittings and I will then finish this thread off.
Here's a few pics from noeyedear on his approach to easing the bearing races.... Gentle heat over the shed stove...he had to move the kettle I see! Lol
I put the swing arm fittings back on but forgot one important item (because I had thrown away the old one and there wasn't anything in the box) and that was the chain slider
OK, so on with the job in hand. Having fitted the bearings in the swing arm, I added extra grease and slipped in the bearing tube. The next job was to put the big washers from the kit into the end caps and, using plenty of grease, popped in the seals. I find it easier to put the seals in the caps and then fit them to the swing arm as they are quite a bit chunkier than the originals.
Swing arm ready to fit. Make sure you fit it the right way up as it fits both ways. I wasn't wide awake this morning (TRF social at the pub last night ) so put mine in upside down and had to take it out again!
Push the bolt through from the RHS, fit the nut and washer and torque it up to a hefty 105Nm.
Fit the link arm to the swing arm and torque to 59Nm.
It was a bit of a faff fitting the chain slider with the swing arm in place but it was possible and saved taking out the swing arm pivot bolt and re-torquing it.
Job done and cuppa time
HINT - try to do the job in one hit to save misplacing or forgetting parts!
When doing my swingarm bearings the second time, I fitted a grease nipple in the swingarm and, before tightening the main bolt, I pumped in grease until it came out around either end. Now it's just a case, now and then, to give a careful top up (as it might be possible to pop the seals out ). No signs of any wear after 2 years of riding
I had to fit another set of swing arm bearings and seals today so tried refining my fitting process as my vice doesn't open wide enough to easily accommodate the swing arm, bearings and sockets needed to press the bearings in .
I used a length of 10mm threaded bar, two large washers, one 17mm Nyloc nut, an ordinary 17mm nut, and a 21mm 1/2" drive socket.
I fixed the Nyloc nut onto one end of the bar and then threaded on the washers and bearings as shown in the pic below. It's important the the "square" end of the bearings are on the outside to give a good surface to press on.
Tighten until the washers are flush with the swing arm.
A socket was then needed to push the bearings in a further 3mm.
Job done!
I would like to make a few improvements to the system as follows:
1. Weld a nut on one end of the threaded bar as the Nyloc started to turn under pressure.
2. Make up a couple of proper aluminium collars to hold everything central and allow the whole installation to be done in one go. See below - just need to find someone to turn a pair up for me. The measurements aren't in proportion as I took a pic of an existing drift to help illustrate what's needed. Anyone have a lathe and do a swap for a made up pair for some TTR spares?
The collar would need a 12.5mm hole through it to accommodate a bigger threaded bar if that was found necessary.
hi, im trying to remove my rear swing arm and i got the nut loose. but the bolt wont slide. i tried hitting with a hammer but no luck. im wondering is there any other tricks to it? or do i just need to hit it harder?
That is normal and you can't rotate the bolt from that side.
Have you tried applying heat and then cooling then applying heat again? This may help free up a rusted in bolt. I spent nearly 2 hours getting 2 engine bolts out the other day and only the heat would get them out.